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After ballasting my track, in the 'standard' way,  several of my RCS turnouts [with non-derail segments] no longer work properly.  Here's what happens:   Pushing either button on the DZ-1002,  or rolling a train over either non-derail segment causes 'flip-flop': i.e., the points rapidly swap between thru & deviation.  The action stops only when either the button is released or the train leaves the non-derail segment.  Obviously, this is unacceptable!

I'm wondering if anyone can explain this....BETTER YET:  How do I fix it????!!!!

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Yep. had the same issue. There is an electrical contact happening. Check the machine to make sure the wires going in and out are not making contact. Also check the rail gaps you cut, still have a gap, or did the glue fill the gap...

I found my wire harness to have small spots of insulation that came off and made contact later on. Had to rip them  out and start over.... 

JD:  Were yours, like mine, working perfectly before ballasting?

OK; I've checked gaps & wires.  Nothing there that I can see. I scraped the ballast from beneath the gaps.  No help.  What's ESPECIALLY strange is that the problem showed up for just 3 of the 70 turnouts that I've ballasted!!!!

Dennis Zander is also stumped, but I'll try a suggestion of his & report back......

What type  of glue did you use? If it's water based it might not be dry .( grab a  hair  dryer)

I had a set of  crossing gated do the same thing with insulated track section and a mixture of dry wall mud for the road crossing. .... Gated were always down until the mud finally dried. It took a long time to completely dry.

Phil, 

yes, mine worked fine then acted up after ballasting and screwing the switch down.  Same situation where the switch would rapidly flutter back and forth when a car would roll over the section.  I cut the insulated pin out and then everything was fine for my switch.  

if you can, check the continuity over the insulated gap, it should tell if that is the problem.  

We had the same problem> I would try this:

Wet  ballast adhesive will definitely cause a short. Use a hair dryer and wait overnight. If that doesn't fix it I would ask, did you nail your track down?  Ours was probably over nailed so we disconnected all power to the tracks and disconnected the non derail wires and the common and zapped them with 120V, Of course you have to be careful. Took a extension cord, cut off the socket end and split the wires. Then fastened them to two wood sticks with about 1/2 in of insulation removed. Touch the wires to the two insulated trigger sections.  If there is a nail or wire making contact this will usually burn the short out with no damage to the track other than a spot where contact is made.  If you get a spark there is/was a short if no spark something else is wrong.  Have a helper do the plug/unplug of the 120V while you touch the track with the hot ends.

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