Progress report on the engine:
- Installed encoder PCB and new flywheel.
- Found that the original flywheel I was going to use didn’t fit in the shell.
- I pulled another flywheel off a personal project that fits perfectly.
- I made a bracket for the RCMC and repurposed the MUX bracket to mount in the shell.
- Installed Flickering Fire box PCB to the motor.
- Installed program/run switch.
- Wired and gave it a initial test