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Short in 60 Trolley (update, well not reallly)

I bought a 60 trolley on the bay for the chassis, but when it arrived it looked in pretty good shape.  I decided to try to resurrect it.  I put in on my test track for a quick check and it started to smoke.  Time to dig in.  I've completely refurbished 3+ trolleys, so I'm pretty comfortable with taking it totally apart and rewiring what's necessary (short of rewinding the field coil and armature).  It was in pretty bad shape with 50+ years of caked on grease and disintegrating wires.  Amazingly the brushes were in great shape.  I cleaned it all up, lubed it, rewired the track rollers and light, and put it on my test setup (alligator clips, no track) with power coming straight from a KW transformer.  The motor and light worked really well in both directions.  Great, time for a track test.

I put it on my track which is powered by a ZW, with a kill switch when shorts are detected.  It tripped the short switch in both directions.  I took it apart again, made sure all connections were secure and no exposed wires were touching anything.  Again, it worked fine with power from the clips.  When I put it on the track, it again tripped the short switch.  So I reset it and tried to power it up slowly with the ZW handle.  The light came on at low power and got brighter as I increased power.  The light would stay on at that point and not trip the switch.  But when I applied more power to get it to go the switch tripped.

The armature seems to be in the worst shape.  You could see some rust on the outside of it.  I rubbed it off the best I could.  Would that be the source of the short?  I do have an ohm meter, but I'm not real good at knowing how to use it.

Last edited by texgeekboy
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