I recently installed an ERR CCM in a KLine A5 switcher. For the most part this installation went well. The A5 moves at slow speeds, the lights and horn work, the couplers work, etc.
However, when using DCS, my usual control system, the engine continues to creep along even when the DCS reads 0. It also frequently doesn't respond to the "Dir" command to stop. I often have a slow motion runaway locomotive.
I experiemented with a recently purchased CAB1 controller. The CAB1 slows the A5 to 0 and causes it to change direction as it should. However, my preference would be to use DCS for everything, as I've used it for a long time.
Any suggestions for making the A5 perform as it should using DCS?
Many thanks for your suggestions!