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I put an older PS2 SW switcher on my layout the other day; it moved for about 30 seconds and then it stopped.  I put the switcher on another loop, and saw it was drawing too many amps. 

I then decided to open it up and investigate it, along with searching the forum for help.  

The pic below from this forum topic, https://ogrforum.ogaugerr.com/...r-ps2-sd60-just-died, is an almost identical view of what I found:

The left-most, blue capacitor is slightly bulged; the red wire and black wire touching the top surface of it are both melted, slightly bare, and stuck to the top of the cap.

My questions are:

1.  Did the red wire & the black wire melt from both being squeezed against the cap, melting away their wire insulation, causing DC voltage to touch and blow the cap?  Or,

2.  Did the capacitor blow from a DC regulator or white PS2 battery issue, thus melting the two wires?

3.  Either way, do I open and inspect my many PS2 engines and move these two wires away from touching the top of the capacitor?

4.  While I am in there, do I replace all of my white PS2 batteries with battery eliminators?

5.  At this point, do I disconnect the wire harness at the DC regulator and put AC to it to verify it works properly?  Finally,

6.  How do I get these PS2 boards apart to change out the capacitor, and see if my switcher can be revived?

Thanks in advance for the responses!

 

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all those ps 2 5 volt boards are unrepairable and cannot not be taken apart successfully! believe someone that has tried, not worth the effort! you can buy a used ps 3 volt board if you can find one  and replace the board and it will work again !only thing is you would also have  to replace the 16 ohm 50mm speaker with a 4 ohm 50 mm speaker and install a 2.4 volt rechargeable battery from an asc tech or mth in Maryland! also u could have n asc tech install a ps 3/2 board and all features will work as before but not cheap the board alone sells only to asc tech and sells for around $300.00 or less! I just finished a l3 mohawk for a client and he love in no more battery to deal with on ps 3/2 board uses a super cap instead!

Thanks, Alan!  My first check was just that; my trusty voltmeter showed roller to ground continuity. 

I am still curious about the root cause.  Did the capacitor overheat and melt the two wires, or did the wires overheat from an amp draw that melted their insulation to short into the cap? 

It's pure speculation on the root cause, it's hard to know if the cap blows and takes something else out, or the diodes inside croak and kill the cap.

I will say, I'll bet the brand name on that cooked cap is WINCAP, I see lots of those popping.  I have had limited success (very limited) in replacing that 330uf 35V cap and reviving these boards.  I've gotten a couple of them back, obviously suggesting the cap was the only failure.  I've also had a couple that the cap was bulged and leaking, but the board was still running.  Needless to say, I replaced the cap on the spot, and for at least two of these, that's solved the problem for several years.

you just crush the capacitor just above where the leads go threw the pc board not to pull to hard or you'll rip the leads out of the circuit board. Usually needle nose plier and crush the bottom of the capacitor but not the leads and remove piece by piece then solder to leads on the capacitor and mount  where ever it will fit. if your not good at these kind of things I would not try to! 

Thanks, John!

I ended up going the "get-it-now" route, and these will be here at my house sometime today:

https://www.amazon.com/330uF-1...ndustrial&sr=1-5

I will give an update on how I fare with this salvage project.  Best case, I get the switcher running again; worst case, I have enough replacement caps to proactively swap out all of the Wincaps in my extensive PS2-5V fleet before powering any more of those engines up!

From the photo, the cap looks ok. Only thing that would melt wires is a short to the metal frame with. Hiigh I draw. I would first find the Nick in the wire insulation and shrink tube over it. I had this happen on Lionel's M7 and MTH SD35 CNJ. Both cases the wheel flange cut into the hot wire on curves. Caps do go bad and puff out at the top. Also, you man notice the yellow chemical on the bottom rubber where the leads are.

 

 

Here is my pic (previous pic was from a similar forum post):

It is tough to make out, but the red wire and black wire were melted to the cap and charred from shorting.  I cleaned them up and put a small piece of 3M electric tape on them.  No other wires, even to rollers, are bare.

The cap is only slightly puffed, but I’m pretty sure it is shot.  I removed the battery and checked the cap for voltage, so going to crush it now.  Update coming.  

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