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Hey Folks,

I have a curious (to me) electrical problem involving a pair of Lionel 022 turnout switches.

The two switches are located 4 feet apart on the layout.  One is a master, and one is a slave.

Both switches have a good constant 14 volt current wire plugged into them.

The controller is a standard Lionel controller. (A tall lever which will toggle back and forth.)

The controller wire (3 wires)  runs straight from the controller to the three poles/contacts of the master switch motor.  From there, a second wire (3 wires) runs from the three poles/contacts of the master switch to the three poles/contacts of the slave switch.

With the track powered up, when I throw the controller lever, in either direction, both switches work great, with a loud snap.  Both sets of the moving rails in the switches click to the other side, nice and tight, with no bounce back or gaps in the closed rails.

And, if I run an engine into one of the forked ends of the Master Switch, and the Master Switch is set to the wrong side, then the automatic non-derailment feature on both switches works great, and both the Master Switch and the Slave Switch click over instantly and tightly, with no problems or gaps in the closed up rails.

HOWEVER,   if I run an engine into one of the forked ends of the Slave Switch, and the Slave Switch is set to the wrong direction, then auto non-derailment feature on the Slave Switch itself works great,  and instantly and tightly switches the rails over, but the rails on the Master Switch only swing over about 90% of the way, and the outer swing rail does not close up tight against the outer rail of the straight rail section of the switch.  This leaves about a 1/8th inch gap between the rails. It is not travelling all of the way over and then bouncing back, it just never gets all of the way over.

The result is that when an engine later comes inbound on the straight section of the Master Switch, trying to continue going straight, it always derails because of this gap.

I have checked the wire connections over and over, and they are all good and tight.   

Long and short:  the automatic non-derailment switching feature on the Slave Switch will not automatically cause the rails of the Master Switch to swing over 100% of the way.

The only visual thing I can see, is that the 3 strand controller wire running from the controller to the Master Switch is all copper, but the 3 strand wire running from the Master Switch to the Slave Switch looks like an aluminum color.  Frankly, I don't know if it is tinned copper or aluminum.

And again, when I work the controller lever, both switches automatically  work great?


Any ideas about what is causing this problem?

Thanks,

Mannyrock

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Your anti derail function depends on ground (outer rail) connection and the wheel set to short out and act as a switch. This is the same thing as the switch controller doing it, but the difference is more components in the circuit and thus higher resistance.

It's probably not the wire.

It's probably the condition of the rail surface, the wheels, the axle and one thing not talked about, the crimps of the rails inside the switch. Again, in simple terms, your drive strength is a function of resistance. You clearly have higher resistance in the circuit that fails. Solve that resistance and the problem goes away. It could be loose track pin fits to the rails of the switch, incorrect insulator pin placement on a common rail that then sees higher resistance.

https://ogrforum.ogaugerr.com/...45#40004360093384045



Again, the fact it wrks fine with the switch controller stand, but then fails on using the sensing anti-derailment rail- given the anti-derail knowingly has more resistance easily explains the failure.

The manual says in the event of irregular or one direction operation only, the trouble may lie in the sliding contact assembly. Examine the riveting of the springs to the insulating base and the base.  While you have the top off, maybe a cleaning of the contacts would help.  Are you 100% sure that the 14V you have plugged into the slave switch is getting to the solenoid, since if it was not, the track voltage would be powering that switch and giving you a false assumption.  A shot in the dark as a suggestion, the control lamps are lit by current passing through the solenoid of the direction that is not selected.  Is there a difference in brilliance depending on direction that might indicate a voltage issue in the whole thing?

@Mannyrock posted:

Hey Folks,





Long and short:  the automatic non-derailment switching feature on the Slave Switch will not automatically cause the rails of the Master Switch to swing over 100% of the way.

And again, when I work the controller lever, both switches automatically  work great?


Any ideas about what is causing this problem?

Thanks,

Mannyrock

The difference between the control lever working and the anti derailment not working is resistance.

The switch controller has 3 wires, common (AKA U or I described as GND) and the 2 wires for either direction. The controller shorts one of the direction wires to common to activate. Since the controller is designed as a proper switch contact with low resistance and positive solid contact.

VS

Anti-derailment sensing rail, which is connected to the specific direction. The thing is, this is a switch that depends on your rolling stock wheels to short this sensing rail to the common (U) connected other rail. Depending on how well that specific rail is tied to common (U), how clean it is, how clean your wheels are, how much weight or pressure, how clean the wheel to axle is, these factors all determine the total resistance seen between the sensing rail and the U common rail.

In your case, you are attaching 2 switch motors and thus 2 switch coils worth of current now has to flow across this anti-derailing sensing connection. That's 2X the current across the wheels and axles as they roll across this to ensure both switch coils fully actuate. Since the near switch coil is right there, it switches because it sees less total resistance than the remote far away switch coil connected via longer wires. As a note, yes, the wire resistance comes into play but I'm of the opinion even thick heavy copper wire may not solve this issue since the primary resistance is the rail to wheel to axle to wheel to rail resistance.

LIONEL POSTWAR O/O27 TRAINS WHEELS & AXLE ROLLING STOCK WHEEL SOLID CAST IRON | eBay

You may not care if running only postwar non-electronic equipment but each time you depend on this switching 2 high current 022 switch motors via you anti-derail sensing, you are possibly sending a massive inductive kickback voltage spike in that general area. Again, I would bet money, with the lights off, there is a decent sized spark or sparks when you activate the switch via ant-derail sensing of the wheels carrying all that current of 2 switch motors at the same time.

Last edited by Vernon Barry

Wow.  Thanks for all of the info.  Lot's of things for me to check into.

Arthur, yes the first thing I did was to pull the switches, thoroughly clean them inside and out, and squirt them with the can of CR whatever.  After reinstalling them, they worked even snappier when the control lever was thrown, but the problem of the incomplete rail throw of the Master Switch continued as before.

I actually thought from the beginning that it was a resistance issue, but didn't have the education to figure it out.  I know that they are both receiving the 14 constant volts because their lanterns are bright when the track throttle is on zero.

I'll try to work through the problem, and if I can't solve it, I guess I'll just put in a separate controller for the Slave switch, put the two controllers side by side on the control board, and somehow "tie" the two controller levers together so they operate in tandem.  After that, the non-derailment functions will have to work independently. 

Thanks again,

Mannyrock

Thanks for the info Rob!

Instead of moving the controller wires to the second switch, I think I can test it the same way by just tripping the second switch by using a thin metal screwdriver to touch an outside post to the interior post.  I can test this on each outside post.

Also, I forgot to mention, that in doing my initial testing, I disconnected all of the controller wires from both switches, so that there was no controller operation, and powered up the transformer so that they were both getting the 14 volt constant flow, and then tested the non-derailment feature on each switch independently, on both track forks on each switch.

The non-derailment feature worked perfectly on each switch.

Thanks,

Mannyrock

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OGR Publishing, Inc., 1310 Eastside Centre Ct, Suite 6, Mountain Home, AR 72653
800-980-OGRR (6477)
www.ogaugerr.com

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