Skip to main content

 I didn't want to cloud a post in the 3 rail forum with another problem. I have a USA trains GP30 G scale engine, that someone else converted to PS2. It has all the stock PS2 guts inside and even MTH trucks. It has always run fast. It runs faster than any other MTH G scale engine I have and won't go in a lashup with any other engine. I have swapped sound files, swapped tach readers, I've cleaned the flywheel which even has painted on MTH stripes. It was the first release of G scale Amtrak Dash 8. It still ran fast. About five scale MPH too fast.

 So when I was running it and it started acting up, I figured something in the board was finally failing.

 

I narrowed a problem down to a dead short in one truck across the wheels and pickups. I noticed that if the bottom removable plastic cover is tightened to much, there's a dead short inside. Sounds easy to find, but I haven't gone farther. I left the cover screws snug and all was well?? It ran good when I ran it.

 Fast forward a few months and I took it off the shelf to run with a new G scale conversion I was doing that must have had a wrong tach tape because it also was running fast. I paced the two engines a foot apart and they ran in sync. Then the GP30 at first slammed to a stop. I restarted it and it ran again in pace with the other. I was about to couple them together when I lost all control of this GP30. It ran silent at the speed it was last running after bucking a bit? It stopped quickly resumed to speed and repeated. It seemed like it wasn't getting the speed command correctly.

 I figured the engine's trucks must be shorting again. I fired the engine up one more time to see if the board was fried because I couldn't detect a short. It fired back up as if the board had recovered again. I have not run it since.

 So.........shweeew. I'm tired of typing.

I figure the only proper thing is to remove the board and test it in another engine? or Should I send it out for safety of the board? Sound like a different component failing? If I install it in a known good engine, I might expect to solve the issue????

 I always thought this board had an issue because of the speed difference. When the truck is shorted, it trips the breaker because the short is dead across the wheels. The breaker never tripped??

Original Post

Replies sorted oldest to newest

The MTH smoke fan motors are twice the size of the O motors so the current draw will be higher.  The fan is powered by the 5V regulator that powers all the micro chips and ultimately the power supply to the main processors.  So if it draws high current, even if just momentarily it can cause the 5V regulator to shutdown. 

 

Got that the guts are the same, but what sound file was loaded?  G

I narrowed a problem down to a dead short in one truck across the wheels and pickups. I noticed that if the bottom removable plastic cover is tightened to much, there's a dead short inside. Sounds easy to find, but I haven't gone farther. I left the cover screws snug and all was well?? It ran good when I ran it.

 

Why not find & fix the short before you wipe out a PS2 board or two?

 

I'm just wondering if the smoke unit's fan was attached to the elements supply, could that shut down the board if it was shorting or drawing too much?

 

Unplug the smoke unit wiring harness from the PS2 boards and then try it out...see if that eliminates any problem. 

Originally Posted by gunrunnerjohn:
Originally Posted by GGG:

The MTH smoke fan motors are twice the size of the O motors so the current draw will be higher. 

Twice the size of what motor?  The smoke fan motor is the smallest motor in the locomotive!

Should have been more clear.  G gauge smoke units are bigger.  They have 3 16 ohm elements in parallel and the smoke fan motor is much larger than the O gauge smoke fan motor.  G

 Ok, let's see.

John it's G scale with G scale MTH guts.

CRH, because it never came up again for months and I got lazy with other projects across my bench.

G, It has a GP30 or GP35 soundset inside right now if I remember?That was in during the shut down.

 I put the original G gauge Dash 8 file back in when I got it and the speed remained fast. So I reloaded the GP soundset for more accurate sounds.

Last edited by Engineer-Joe

 The condition of the MTH flywheel I would say is perfect. I was concerned about grease as the flywheel is down in there with the gear box. I cleaned it and it did not make any difference.

 I had considered a new tape with a correction in the number of stripes. I didn't think it would survive if the grease got to it. I figured I would just keep this engine as a lone switcher until it acted up.

 I'm in the process now of converting another engine. When it's done and I'm sure there's no problems, I'll install this board for a test run. It should be nice weather by then and I can run it harder out back! I like the idea of trying it without the smoke unit connected as a further test. I have trouble narrowing down electrical problems that are intermittent like this one.

Originally Posted by GGG:
Originally Posted by gunrunnerjohn:
Originally Posted by GGG:

The MTH smoke fan motors are twice the size of the O motors so the current draw will be higher. 

Twice the size of what motor?  The smoke fan motor is the smallest motor in the locomotive!

Should have been more clear.  G gauge smoke units are bigger.  They have 3 16 ohm elements in parallel and the smoke fan motor is much larger than the O gauge smoke fan motor.  G

But that's only if the conversion is using a MTH G Gauge smoke unit. A Lot of conversions that I've done use smaller USA Trains smoke units which are comparable to a O gauge type. Only room for 2 heaters in those. The big MTH One-Gauge Big Boy smoke units have room enough for 3 or more heaters.

Originally Posted by Enginear-Joe:

 The condition of the MTH flywheel I would say is perfect. I was concerned about grease as the flywheel is down in there with the gear box. I cleaned it and it did not make any difference.

 I had considered a new tape with a correction in the number of stripes. I didn't think it would survive if the grease got to it. I figured I would just keep this engine as a lone switcher until it acted up.

 I'm in the process now of converting another engine. When it's done and I'm sure there's no problems, I'll install this board for a test run. It should be nice weather by then and I can run it harder out back! I like the idea of trying it without the smoke unit connected as a further test. I have trouble narrowing down electrical problems that are intermittent like this one.

Shutting down and slamming to a stop ain't good. Some MTH PS2 boards will do that for no reason...Seems Barry B. once commented on this problem a year or so ago. I had a One-Gauge Hudson that would do that for no reason. Could almost set your watch by how often that thing would shutdown...and it would stop at dang near the same spot on the layout every time. I had about 50 other loco's that wouldn't do that...only that Hudson..those boards got swapped out and went into some O Gauge engine.

Originally Posted by CRH:
Originally Posted by GGG:
Originally Posted by gunrunnerjohn:
Originally Posted by GGG:

The MTH smoke fan motors are twice the size of the O motors so the current draw will be higher. 

Twice the size of what motor?  The smoke fan motor is the smallest motor in the locomotive!

Should have been more clear.  G gauge smoke units are bigger.  They have 3 16 ohm elements in parallel and the smoke fan motor is much larger than the O gauge smoke fan motor.  G

But that's only if the conversion is using a MTH G Gauge smoke unit. A Lot of conversions that I've done use smaller USA Trains smoke units which are comparable to a O gauge type. Only room for 2 heaters in those. The big MTH One-Gauge Big Boy smoke units have room enough for 3 or more heaters.


Early on he stated all MTH guts, including trucks transplanted.  G

Originally Posted by CRH:
Originally Posted by Enginear-Joe:

 The condition of the MTH flywheel I would say is perfect. I was concerned about grease as the flywheel is down in there with the gear box. I cleaned it and it did not make any difference.

 I had considered a new tape with a correction in the number of stripes. I didn't think it would survive if the grease got to it. I figured I would just keep this engine as a lone switcher until it acted up.

 I'm in the process now of converting another engine. When it's done and I'm sure there's no problems, I'll install this board for a test run. It should be nice weather by then and I can run it harder out back! I like the idea of trying it without the smoke unit connected as a further test. I have trouble narrowing down electrical problems that are intermittent like this one.

Shutting down and slamming to a stop ain't good. Some MTH PS2 boards will do that for no reason...Seems Barry B. once commented on this problem a year or so ago. I had a One-Gauge Hudson that would do that for no reason. Could almost set your watch by how often that thing would shutdown...and it would stop at dang near the same spot on the layout every time. I had about 50 other loco's that wouldn't do that...only that Hudson..those boards got swapped out and went into some O Gauge engine.


Sounds like the main rectifier shutting down.  I repaired one where the board did not have any special changes for 1 gauge.  MTH does make a special board with the rectifier wired in so it can be heat sinked to the chassis, and a larger flyback diode that also can be heat sinked.  G

Last edited by GGG
Post
The DCS Forum is sponsored by

OGR Publishing, Inc., 1310 Eastside Centre Ct, Suite 6, Mountain Home, AR 72653
800-980-OGRR (6477)
www.ogaugerr.com

×
×
×
×
Link copied to your clipboard.
×
×